The Carryfast engine design discussion

newmercman:
The Rolls Royce engine was the third choice engine among ERF, Foden and Seddon Atkinson customers, this is true, but that doesn’t mean that it was an inferior product and those companies were not major competitors to Leyland in sales terms, their combined output was less than Leyland and would’ve been even less had RR become the in house engine supplier to Leyland.

The fact that both companies were being bailed out by GB Ltd makes a merger a no brainer in financial terms, in engineering terms it also made sense as proven by the lifespan of the basic design.

I’m convinced that Leyland would still be producing truck and bus chassis today if they hadn’t committed commercial suicide in the 70s. And it was the heavy trucks that were the problem, the Roadrunner was a fantastic little lorry, the Freighter was more than the equal to the foreign competition, the Scammell Constructor six and eight wheelers were second to none too, it was only the Roadtrain that let the side down and that wouldn’t have happened if it had the right driveline from the start.

That 300hp tractor unit market was the one that really established the competition, the F10, 112, 3300, E290, L10 etc and the T45 as it was had no chance, had it been launched with a full range of cab options, a 265hp to 320hp engine range and a 9/10/13spd Fuller, it would’ve been a very different story, one that had a happy ending.

^
We’re finally on the same wavelength. :smiley:

Which just leaves the question ■■■■ up or conspiracy.
It really was a special type of stupid just too special to be true.
The smoking gun is the question why the big need to split up the truck and bus division ( knowing what happened next ).

While keeping BMC tied round the Group’s neck.Then going full ■■■■■■ by thinking that the SD1, Triumph Acclaim and Rover 820 were the logical competitors to BMW 3 and 5 series. :open_mouth:

I would’ve split truck and bus for the reasons I said above, why they did God only knows, as you say the decisions made were beyond stupid, it’s as if it was deliberate sabotage.

Was it capitulation to the EEC? I don’t know, but they had no problem giving our fish away decimating that industry, why not the automotive and truck and bus industries too.

newmercman:
I would’ve split truck and bus for the reasons I said above, why they did God only knows, as you say the decisions made were beyond stupid, it’s as if it was deliberate sabotage.

Was it capitulation to the EEC? I don’t know, but they had no problem giving our fish away decimating that industry, why not the automotive and truck and bus industries too.

As I’ve said numerous times and been prepared to face the flak for it I was there in the day on the front line with some of the best workers it was my privilege to know and speak to.Of a generation that this country could never repay for what they did for us.
Then the lucky ones who came home dragged our smashed and battered country and economy up off its feet and rebuilt it.
With the bankers and government working against them and for their European competitors.
They told me that and I believe every word of what they told me.
They had no reason to lie what would have been the point.

The Marshall Plan was a bit of a kick in the teeth for veterans, that’s for sure.

And we could have moved the RR manufacturing plant and machinery from Shrewsbury to Southall to replace the clapped-out engine manufacturing line there. It was virtually all new machinery at Shrewsbury when RR went bust. (Did Shrewsbury have a foundry for making its own castings does anyone know?)

gingerfold:
And we could have moved the RR manufacturing plant and machinery from Shrewsbury to Southall to replace the clapped-out engine manufacturing line there. It was virtually all new machinery at Shrewsbury when RR went bust. (Did Shrewsbury have a foundry for making its own castings does anyone know?)

There was still a foundry there. I had a week there in 1981 and we were shown around the works. Of course like Fodens Sentinel had been makers of steam powered vehicles (and railway engines) so a foundry was essential, it was like Elworth Works really and still had the Victorian air about the place!

Also, despite being involved in engine rebuilding for 15 years I learned new ways of doing things like fitting wet liners differently to how I had always done it.

Pete.

gingerfold:
And we could have moved the RR manufacturing plant and machinery from Shrewsbury to Southall to replace the clapped-out engine manufacturing line there. It was virtually all new machinery at Shrewsbury when RR went bust. (Did Shrewsbury have a foundry for making its own castings does anyone know?)

^ That’s also my view of how such a buyout would/should have gone.

Whatever it had Vickers and then Perkins were no fools.They saw something worth taking a punt on.By all accounts the sale to Perkins was very lucrative for Vickers’ shareholders.

While at this point were Leyland in the process of moving AEC’s engine production operations to Leyland as part of the ‘AEC’ closure ( eventual DAF and Volvo handover ) plan ?.

The whole scenario couldn’t have worked out better for those two competitors almost as if it was being orchestrated by them.

windrush:

gingerfold:
And we could have moved the RR manufacturing plant and machinery from Shrewsbury to Southall to replace the clapped-out engine manufacturing line there. It was virtually all new machinery at Shrewsbury when RR went bust. (Did Shrewsbury have a foundry for making its own castings does anyone know?)

There was still a foundry there. I had a week there in 1981 and we were shown around the works. Of course like Fodens Sentinel had been makers of steam powered vehicles (and railway engines) so a foundry was essential, it was like Elworth Works really and still had the Victorian air about the place!

Also, despite being involved in engine rebuilding for 15 years I learned new ways of doing things like fitting wet liners differently to how I had always done it.

Pete.

Thanks for that Pete. Leyland had its own foundry at Faringdon, and again they made steam waggons in the early days. AEC never had a foundry at either Walthamstow or Southall. Castings were bought in from both Leys and Qualcast.

Extracts from an article written by Robert Smith, entitled “Memories of Working at AEC”, published in the AEC Bulletin. June 2015.

Robert was a fitter / driver who drove the test vehicle on nights with the development TL12 engine, or AV770 as it was known at AEC.

Robert writes: -
My recollections of the two VTG tractor units are limited as I had nothing to do with them until they became the test bed vehicles for endurance testing the Marathon’s engine.
These two chassis and cabs had been built in our experimental workshops; both were 6x4 units. One had had a naturally aspirated V8 while the other had a twin-turbo charged V8. I never drove either of these vehicles with these engines, much to my disappointment.
The V8s were removed from both 3VTGs and 770 (TL12) engines were fitted in their place. One was cut down to a 4x2 unit. The 6x4 unit had a gross weight of 44 tons, of which 31.5 tons was payload. We had special permits to run at this weight on a designated route.
It was on the road 6 days and nights a week for 50,000 miles. Then the engine was removed and transferred to Engine Research where it was totally dismantled, all items measured and rebuilt, returned and re-fitted to the chassis for another 50,000 miles. I can’t recall having any trouble when I was driving it.
The night shift, 8.00 pm to 7.00 am, consisted of leaving the works, going through Hayes End to J3 of the M4, and then M4 to Severn Bridge, turning round and coming back to J8/9 Maidenhead, turning round, and back to Severn Bridge again, and then returning to Southall. That gave a total of 385 miles for each shift.
After Aust Services, coming towards the M4/M5 interchange, you come up a hill, and one night a truck and trailer was about half way up when I was at the bottom. I overtook him near the top and thought no more about it. I stopped at Leigh Delamere services as usual for my break. Sitting at a table on my own the driver I overtook earlier came and asked if I was driving the big white-cabbed truck with the test weight load. I replied “yes”, he said he had seen me at the bottom of the hill coming up fast behind him and he thought I was empty. He was surprised to see I was loaded and astonished to learn what weight I was carrying. He asked what my slowest speed was up the hill. It was 17 mph, his was 10 - 11 mph.
On the level I could maintain 64-65 mph, and that was with a 6x4 unit, when it came to hills I overtook everything that was loaded. At Leigh Delamere there were always five Marks and Spencer drivers taking their breaks at the same time as me. They had Guy Big Js with AEC AV505 engines, and pulling single axle trailers at 22 tons gross. I used to give them 5 minutes start then set off after them. Over the period of the next hour I would overtake all five of them, one or two at a time, and always going uphill, never on the flat. Well it was a little bit of excitement in a long boring run.
I used to leave Leigh Delamere between 3 - 3.30 am on the final run home. On this particular night I was climbing up one of the hills between Swindon and Newbury when a Foden 8-wheeler started to overtake me - he was partly loaded; he was just about past me when the hill got steeper, and he fell back a bit, then the hill got less steep and our speeds were rising and he started to overtake me again. Our cabs were about level when the turbocharger started to whine, and when that happened it gave extra engine power and I was away, not quite in a cloud of dust but I never saw him again after that.

End of the extract.

I would hazard a guess that no other engine manufacturer in the UK was testing a new engine design at 44 tons gvw in 1973. Make of that extract what you will.

gingerfold:
Extracts from an article written by Robert Smith, entitled “Memories of Working at AEC”, published in the AEC Bulletin. June 2015.

Robert was a fitter / driver who drove the test vehicle on nights with the development TL12 engine, or AV770 as it was known at AEC.

Robert writes: -
My recollections of the two VTG tractor units are limited as I had nothing to do with them until they became the test bed vehicles for endurance testing the Marathon’s engine.
These two chassis and cabs had been built in our experimental workshops; both were 6x4 units. One had had a naturally aspirated V8 while the other had a twin-turbo charged V8. I never drove either of these vehicles with these engines, much to my disappointment.
The V8s were removed from both 3VTGs and 770 (TL12) engines were fitted in their place. One was cut down to a 4x2 unit. The 6x4 unit had a gross weight of 44 tons, of which 31.5 tons was payload. We had special permits to run at this weight on a designated route.
It was on the road 6 days and nights a week for 50,000 miles. Then the engine was removed and transferred to Engine Research where it was totally dismantled, all items measured and rebuilt, returned and re-fitted to the chassis for another 50,000 miles. I can’t recall having any trouble when I was driving it.
The night shift, 8.00 pm to 7.00 am, consisted of leaving the works, going through Hayes End to J3 of the M4, and then M4 to Severn Bridge, turning round and coming back to J8/9 Maidenhead, turning round, and back to Severn Bridge again, and then returning to Southall. That gave a total of 385 miles for each shift.
After Aust Services, coming towards the M4/M5 interchange, you come up a hill, and one night a truck and trailer was about half way up when I was at the bottom. I overtook him near the top and thought no more about it. I stopped at Leigh Delamere services as usual for my break. Sitting at a table on my own the driver I overtook earlier came and asked if I was driving the big white-cabbed truck with the test weight load. I replied “yes”, he said he had seen me at the bottom of the hill coming up fast behind him and he thought I was empty. He was surprised to see I was loaded and astonished to learn what weight I was carrying. He asked what my slowest speed was up the hill. It was 17 mph, his was 10 - 11 mph.
On the level I could maintain 64-65 mph, and that was with a 6x4 unit, when it came to hills I overtook everything that was loaded. At Leigh Delamere there were always five Marks and Spencer drivers taking their breaks at the same time as me. They had Guy Big Js with AEC AV505 engines, and pulling single axle trailers at 22 tons gross. I used to give them 5 minutes start then set off after them. Over the period of the next hour I would overtake all five of them, one or two at a time, and always going uphill, never on the flat. Well it was a little bit of excitement in a long boring run.
I used to leave Leigh Delamere between 3 - 3.30 am on the final run home. On this particular night I was climbing up one of the hills between Swindon and Newbury when a Foden 8-wheeler started to overtake me - he was partly loaded; he was just about past me when the hill got steeper, and he fell back a bit, then the hill got less steep and our speeds were rising and he started to overtake me again. Our cabs were about level when the turbocharger started to whine, and when that happened it gave extra engine power and I was away, not quite in a cloud of dust but I never saw him again after that.

End of the extract.

I would hazard a guess that no other engine manufacturer in the UK was testing a new engine design at 44 tons gvw in 1973. Make of that extract what you will.

I`ve seen that article before Graham and was fascinated the first time i read it, running at 44 tons at 273bhp it sounded like a good performance. What some people fail to remember is that at the time of testing the majority of top weight lorries were low powered so well down the box on every hill so it would have been a bit special just like the V8 was and the F88s and 110s

Extract from an article entitled “The Enigma of the AEC V8 Engine - Why was it ever Produced” written by Bob Fryars, Chief Engineer of AEC and Leyland Truck & Bus, for the AEC Bulletin, June 2014.

Extract:
Why did AEC in the mid-1960s put considerable talent and investment into designing and manufacturing a new engine and accompanying chassis models that were in direct competition to highly successful units already in production? I believe I can throw some light on this puzzle.
Previously I have explained the background to Guy Motors’ bankruptcy, their acquisition by Jaguar, and the attempt to entice ■■■■■■■ to manufacture their V6 and V8 engines in the old Meadows factory next door in Wolverhampton. Sales of loose engines to such as Dodge and Guy had become an important part of AEC’s business, so John Bowley, AEC’s general manager must have wasted no time in telling Lofty England of Jaguar / Daimler that AEC could match ■■■■■■■■ So the concept of making a V engine was launched.
This was in 1961 when discussions on AEC becoming part of BMC were well advanced. I had found that our two truck ranges were a good fit together. It was clearly ACV’s strategy that to meet the coming threat from big continental manufacturers in the Common Market, AEC must become part of a big group for economies of scale. So when John Bowley requested a V engine study he clearly had in mind also broadening the range of industrial engines AEC could offer. The dry-liner version of the AV690 to become the AV691 and the 760 was well in hand as were plans to do the same for the AV470 to meet rising demands on power output.
When Keith Roberts and I obtained copies of the ■■■■■■■ V engine patents we found these cleverly covered the best cylinder bore to stroke ratios. To avoid the patents meant either a long stroke tall V, or a squat over square V engine. We quickly decided a V6 would be a very rough unit at the 90 degrees V essential to fit in a chassis - and ruled out that option. So we were looking at a very over-square V8, one well outside any known direct injection combustion chamber relationship. Then there was noise. Theo Priede, than at CAV, had recently come up with an empirical formula linking diesel engine noise emissions to the square of cylinder bore diameter and to rotational speed. An over-square diesel would be a very noisy unit, which added to the difficulties.
John Bowley proposed a compromise. To deal with technical aspects we should make a short-stroke in-line research engine. We should only scheme a design for a V8 and check that it could be accommodated under BMC’s new FJ cab. Bowley had his V8 brochure by the late spring of 1962 (but no engine!) - a time of turmoil in the motor industry with a disastrous outcome for the future of AEC.
Late in 1961 Rolls Royce had complicated matters by proposing how a tripartite arrangement could be made with ACV. This was soon discounted and ACV merger talks with BMC continued, only to be discontinued when financial forecasts for BMC were shown to be dire. By then ACV had discounted possible mergers with such as Scania, leaving Leyland, reluctantly as the only possible partner.
But the AEC board may not have been aware that at the very same time Leyland was in serious difficulty with its purchase of Standard Motors that could become a catastrophe big enough to bankrupt Leyland itself. Chrysler had arrived on the scene intending to buy a share in Leyland.
August 1962 and the “merger” with Leyland was quickly concluded, much to the dismay of middle management at AEC. I had to make a presentation to the new group board about the development of the 760 and 520 engines, which was scaled back to become the 505. The V8 project, still a brochure at this stage, was mentioned in passing, but nothing more was heard about it for more than two years.
Following this presentation and policy meeting, much later I discovered that in total secrecy Stokes had ordered all further AEC engine development to be stopped in favour of new Leyland designs - The Tattersall Engine.
Norman Tattersall from Leyland Motors had designed, working in secrecy, concept tank engines, based on the Leyland L60, which incorporated “throw-away” cylinder blocks, and with all gear-driven accessories to eliminate belts. Sight unseen of any actual engine Stokes persuaded the board to approve building and equipping a new facility to produce 300 Tattersall engines weekly. But when the 700 (as it was called) prototype engines were tested they suffered major structural failures within hours. But the unusual shape and weight precluded its installation in any Leyland Motors Truck or Bus model. (Except an old bonneted Beaver).
Donald Stokes instructed Dr Albert Fogg to salvage something from this impending disaster, and with input from Ricardo the Tattersall engine was re-designed to at least run satisfactorily. But it was still too big to fit in any normal chassis. This concept was dead in the water, so a scaled down version which became the 500 Series was designed. Naturally aspirated it would produce 160 - 170 bhp, but not powerful enough for the proposed 32 tons legislation impending for 1965.
So why, in this quite dreadful scenario of a failed secret Leyland engine strategy, did attention suddenly turn to the AEC V8? A new updated concept paper was demanded urgently to show a V8 installation under the new Ergomatic cab.
What objective had Donald Stokes and Bertie Fogg in mind? I do not think we shall ever know for certain, since Stokes never put on paper a record of the verbal instructions he gave. Bertie Fogg would never, ever discuss the question. I had to assume that his job would have been on the line if he had ever breathed a word about this Leyland Motors disaster. The AEC V8 “brochure” engine was rapidly rushed through development and into production. The later V8-810 version with Mac Porkess in charge of development at Southall was showing great promise as a turbo-charged unit at 350 bhp, but noise was still a problem and I had to pull the project in favour of the TL12, which at 280 bhp fulfilled our immediate needs in the mid-1970s.
In conclusion I believe the V8 only ever came into production as a second string solution to the almost unbelievable shambles that that the highly secretive Tattersall engine concepts had produced at Leyland. So I have always been proud of how well AEC people designed and developed the V8 and walk-through Ergomatic cab.
But an over-square V8 was never going to be capable of meeting noise, and later, emissions regulations. On both counts, diesel engine bore-stroke relationships would optimise at very conventional ratios for all vehicle applications.

End of Extract.

There is plenty more in this article worth reading, so I have selected what I think are the relevant parts. Suffice it to say… one disaster begats another disaster.

I would imagine that the collosal amount of warranty claims that the BMC commercial vehicle division had regarding the 5.1/5.7 UD and JUJ engines in the FJ and Laird ranges between 1964 and 1970 must have hemorrhaged a vast amount of money from the group as well? That dragged on for several years.

Pete.

Extremely thought provoking articles Graham, thanks for digging them out. So it would appear that the Rolls Royce idea was discussed long before Carryfast and I dreamed it up. If only they had taken that path, Daf may have had to go back to making trailers instead of dominating the European truck market.

gingerfold:
Extract from an article entitled “The Enigma of the AEC V8 Engine - Why was it ever Produced”

There is plenty more in this article worth reading, so I have selected what I think are the relevant parts. Suffice it to say… one disaster begats another disaster.

Firstly the idea that bore stroke ratios/dimensions could ever have been legally patented makes no sense.

Also strangely no mention of the leverage advantage of maximising stroke dimensions mentioned there.As though they’d never even given that any thought both regarding 6 cylinder or 8 cylinder types ?. :confused:

While surely the suggestion that Leyland wanted to emulate the Mack Maxidyne in the TL12’s design brief ? would also have been expected to provide the clue that noise and emmissions wasn’t the whole story in meeting a target of 100 lb/ft + per litre.Or the fact that the TL12’s, let alone V8’s leverage disadvantage v the Maxidyne, wasn’t going to cut it.
IE on the back foot before it even had a turbo, let alone an intercooler, bolted to it.

All that seems to show ‘how’ Leyland ended up with a lesser product than the Eagle.But doesn’t explain why they wouldn’t have wanted to discard the TL12 and do whatever it took to get the Eagle onto their inventory instead by the late 1970’s.

Combined with the suggestion that Leyland’s designers were in fear of their positions and with it reputations if they dared to make any critical observations regarding what they were being instructed to do.

The perfect storm for any nefarious agenda of sell out being imposed from much higher up the chain of command at whatever point. :bulb:

You’re back to the madness again CF. From my interpretation of those posts it appears that internal politics had as much to do with the downfall of BL truck and bus as government interference did. It was like putting a bunch of cats in charge of the chicken barn, absolute pandemonium ensued and we all know the end result.

I’m quite sure a merger between Scania and Volvo would’ve been just as disastrous had one or the other been the dominant partner, pushing through their innovations to the detriment of the whole group.

I’m with you 100% on the patenting of bore and stroke ratios, that is absurd, it’s like getting a patent for the concept of the camshaft ffs.

newmercman:
Extremely thought provoking articles Graham, thanks for digging them out. So it would appear that the Rolls Royce idea was discussed long before Carryfast and I dreamed it up. If only they had taken that path, Daf may have had to go back to making trailers instead of dominating the European truck market.

Didn’t see that exact conclusion reached in there although obviously that’s the implication regarding both TL12, let alone V8, by the time T45 was on the drawing board ?.
Also think that their reference to the eventual need for a return to ‘conventional’ bore stroke ratio’s ( deliberately ? ) left out the leverage side of the equation as though the article had been made under implied duress to avoid any embarrassing questions directed towards Leyland’s management in that regard ?.

For obvious reasons in view of previous mention of a seeming regime of fear permeating the design departments.

My guess is too scared to tell it like it was.In that in the absence of the resources or will at the top to re engineer the TL12 with at least a 6 inch stroke.Then getting our hands on the Rolls Eagle, as Scammell seem to have concluded, will be our best if not only hope before signing off the T45 for production.
Ironically by that point my guess is that AEC had already been earmarked for closure anyway.Thereby also conveniently burying all the inconvenient evidence that the T45 was going to be deliberately nobbled on launch day.
The questions why didn’t Scammell want Leyland’s own in house engine in their Crusader before that point and what did Leyland see in using it in the T45 that Scammell didn’t in the Crusader, being a smoking gun.
Let alone the circumstances of what happened next regarding the sale of Rolls Royce diesels to Vickers and later Perkins.Combined with the fate of Leyland’s truck and bus division.

We know how the bloody Yanks like to resort to court claims about the price of fish and here it is:

courtlistener.com/opinion/1 … rporation/

newmercman:
You’re back to the madness again CF. From my interpretation of those posts it appears that internal politics had as much to do with the downfall of BL truck and bus as government interference did. It was like putting a bunch of cats in charge of the chicken barn, absolute pandemonium ensued and we all know the end result.

I’m quite sure a merger between Scania and Volvo would’ve been just as disastrous had one or the other been the dominant partner, pushing through their innovations to the detriment of the whole group.

I’m with you 100% on the patenting of bore and stroke ratios, that is absurd, it’s like getting a patent for the concept of the camshaft ffs.

But the claim of a patent on bore stroke dimensions came from the AEC side.It just ruins the credibility of AEC’s position whether V8 or TL12 from that point.

What we do know is that Leyland pushed on with the resulting two AEC designs.
The V8’s design being a case of seemed like a good idea at the time followed by oh zb Cosworth DFV F1 race engine design practice ain’t going to work in a 32 tonner.Forget that.

The TL12’s being a case of we’ve got this lump with the same stroke as a 7.5t Routemaster bus motor.It ain’t ideal.But should be ok with some more development and a turbo bolted to it hopefully might be as good as the Maxidyne.
Someone at Scammell says we don’t think so.We prefer this Rolls Eagle that we’re using instead.Both Rolls and Leyland being under government control/ownership at the time.
The rest is history.

gingerfold:
And we could have moved the RR manufacturing plant and machinery from Shrewsbury to Southall to replace the clapped-out engine manufacturing line there. It was virtually all new machinery at Shrewsbury when RR went bust. (Did Shrewsbury have a foundry for making its own castings does anyone know?)

At a bit of a tangent to your foundry question, I can tell you that through the 90s LKW Walters regularly offered loads of new engine blocks from a foundry in northern Bavaria, Nuremburg, Regensburg area I forget precisely back to Sentinel Works, however to the best of my knowledge they were always Vs for military and industrial applications, never an inline Eagle.

Bloody lawyers. Engineers can make do with a pair of numbers. Multiply them together and you get another number. All of those numbers can be made useful. That lot of parasites turn the whole argument into a festival of inconsequential words, for their own benefit. Plough them into the ground.

What was the conclusion of the case linked by cav551? Did ■■■■■■■■ patent on a range of stroke/bore ratios hold up? I apologise for losing my attention while reading the article.